乙烯工业 ›› 2023, Vol. 35 ›› Issue (4): 61-64.

• 压缩机 • 上一篇    

裂解气压缩机长周期运行瓶颈问题与优化措施

张志飞,董亚龙,张立国,王吉利,肯吉别克·夏木西   

  1. 中国石油天然气股份有限公司独山子石化分公司,新疆 独山子 833699
  • 收稿日期:2022-09-06 修回日期:2023-10-01 出版日期:2023-12-25 发布日期:2023-12-19
  • 作者简介:张志飞,男,2011年毕业于石河子大学应用化工技术专业,现从事工艺技术管理工作,工程师。

Bottleneck Problems in Long Period Operation of Cracking Gas Compressor and the Optimization Measures

Zhang Zhifei, Dong Yalong, Zhang Liguo, Wang Jili, Kenjibieke•Xiamuxi   

  1. PetroChina Dushanzi Petrochemical Company, Dushanzi, Xinjiang, P.C.833699
  • Received:2022-09-06 Revised:2023-10-01 Online:2023-12-25 Published:2023-12-19

摘要: 独山子石化220 kt/a乙烯装置裂解气压缩机在2021年检修开工后,机组连续运行11个月,出现了一段吸入压力高、压缩机M因子上涨、段间冷却器结垢等问题,通过优化压缩机洗油介质和更换阻聚剂,有效预防M因子增长,延缓压缩机叶轮及流道结焦趋势,针对裂解气压缩机段间冷却器压差上涨,通过增加隔离阀,实时监控压差趋势,单台切除清焦,有效降低了段间阻力降对压缩机功率的影响。

关键词: 裂解气压缩机 , 结垢  优化措施

Abstract:

The cracking gas compressor of the 220 kt/a ethylene plant of PetroChina Dushanzi Petrochemical Company was put into operation in 2021 after overhaul. After 11 months of continuous operation, some problems emerged such as the high first-stage suction pressure, the increased M factor of compressor and the fouling of interstage cooler. By optimizing the wash oil medium of compressor and changing the polymerization retarder, the M factor growth was effectively prevented, and the coking trend of compressor impeller and flow path was delayed. In view of the rising pressure difference of interstage cooler of cracking gas compressor, the influence of interstage resistance drop on compressor power was effectively reduced by installing isolation valve, monitoring pressure difference trend in real time and switching off a single furnace for decoking.

Key words: cracking gas compressor, fouling; optimization measure