Ethylene Industry ›› 2020, Vol. 32 ›› Issue (4): 60-64.
• CATALYST,SOLVENT AND ADDITIVE • Previous Articles
Ma Shilin, Qin Hailiang, Wang Xiaogang
Received:
Revised:
Online:
Published:
Abstract:
Since the 460 kt/a ethylene plant at PetroChina Lanzhou Petrochemical Company was started up after its overhaul in 2016, the activity of catalysts in the first stage of acetylene hydrogenation reactor has decreased significantly. Based on the statistical analysis of the operation data of the plant in this maintenance cycle, it was found that the coking on catalyst surface caused by temperature runaway and the formation of a large amount of green oil were the main reasons for the decrease in activity of acetylene hydrogenation catalyst. Compared with the previous cycle, the higher contents of acetylene and MAPD and the more C4 components and potential heavy metal in the feed also accelerated the deactivation of catalysts. According to the actual situations, some suggestions for optimizing the operation of the plant were put forward.
Key words: C2 , hydrogenation, catalyst, deactivation, optimal operation
Ma Shilin, Qin Hailiang, Wang Xiaogang. Operation Analysis of C2 Hydrogenation Catalyst in Ethylene Plant[J].Ethylene Industry, 2020, 32(4): 60-64.
0 / / Recommend
Add to citation manager EndNote|Reference Manager|ProCite|BibTeX|RefWorks
URL: http://yxgy.sei.com.cn/EN/
http://yxgy.sei.com.cn/EN/Y2020/V32/I4/60
Operation Analysis and Optimization Measures for Front-end Depropanization and Front-end Hydrogenation Process
Analysis of the First Regeneration Process of Mixed C4 Hydrogenation Catalyst
Progress in Synthesis of Ethylene Oxide from Ethylene #br#
Startup Optimization of Pyrolysis Gasoline Hydrogenation Unit Using High Sulfur Naphtha
New Progress in the Production Technology of Low Carbon Olefin
Problems in Hydrogenation of Raffinate C5 and the Countermeasures
Cited