乙烯工业 ›› 2019, Vol. 31 ›› Issue (2): 34-37.

• 工业技术 • 上一篇    下一篇

1 000 kt/a乙烯装置丙烯精馏塔增产增效操作的优化

张成龙,蒋鹏飞,张  乐,岳  祥,杜新民   

  1. 中国石油天然气股份有限公司独山子石化分公司,新疆 独山子 833699
  • 收稿日期:2018-09-07 修回日期:2019-05-08 出版日期:2019-06-25 发布日期:2019-06-28
  • 作者简介:张成龙,男,2014年毕业于东北石油大学化学工程与工艺专业,工学学士,主要从事乙烯装置生产运行工作,助理工程师。

Optimization of Propylene Rectification Tower in 1,000 kt/a Ethylene Plant for Yield Increase and Efficiency Increase

Zhang Chenglong, Jiang Pengfei, Zhang Le, Yue Xiang, Du Xinmin   

  1. PetroChina Dushanzi Petrochemical Company, Dushanzi, Xinjiang, P.C.833699
  • Received:2018-09-07 Revised:2019-05-08 Online:2019-06-25 Published:2019-06-28

摘要: 中国石油天然气股份有限公司独山子石化分公司1 000 kt/a乙烯装置工艺设计中,丙烯精馏塔塔顶得到纯度(体技术分)为99.60%的聚合级丙烯产品,其中甲烷+乙烷+丙烷含量小于4 000 mL/m3;塔釜分离出循环丙烷,其中丙烯含量(体积分数)要求控制在7%~16%。通过2017年第一季度对丙烯精馏塔运行操作的调整,改变塔釜温度和回流量,使得丙烯精馏塔在保证塔顶产品合格的前提下,塔釜循环丙烷中丙烯含量(体积分数)降至2.5%~11%,同时延长了裂解炉的运行周期,推进了乙烯装置的节能降耗工作。

关键词: 丙烯精馏系统 ,  , 操作优化 ,  , 节能增效

Abstract:

In the process design of the 1,000 kt/a ethylene plant at PetroChina Dushanzi Petrochemical Company, polymer grade propylene with a purity of 99.60 v% is obtained from the overhead of propylene rectification tower, of which the methane, ethane and propane content is less than 4,000 mL/m3. Cycle propane is separated from the tower bottom, of which the propylene content is to be controlled between 7 v% and 16 v%. By adjusting the operation of the propylene rectification tower in the first quarter of 2017, the bottom temperature and reflux were changed, so the propylene content of the bottom cycle propane was reduced to 2.5 v%~11 v% under the premise of guaranteeing the quality of overhead product. At the same time, the operation cycle of cracking furnace was prolonged and the energy saving and consumption reduction of ethylene plant was promoted.

Key words: propylene rectification system, operation optimization, energy efficiency